26-Apr-2024, 04:10 PM
Hello! i just recently got back into RC drones again after a loonngg break. Having some issue with my drone
Cinelog25 - Betaflight 4.5, Bluejay 16.2
Radiomaster boxer
DJI system
I am not sure if anyone can help me, i am trying to figure out why 1 (back Left or Right) motor goes 100% and the other 3 motor stays the same when Throttle down 0%. This happens when trying to do a roll or pitch flip at 0% throttle (when i pump down after hard throttling up).....Here is the funny part, if i dont drop throttle to 0% and hold maybe ard 35%-40% throttle, the motor desync wont happen. Motor Idle too low?
link to BBL file - https://drive.google.com/file/d/1kUi...ew?usp=sharing
I do have BB log (link above) but im not sure if that will help. I took a screen cap to show exactly when it occured (refer below). I am unable to figure out what could be the problem and any input is much appreciated. Thanks!
mojo
Cinelog25 - Betaflight 4.5, Bluejay 16.2
Radiomaster boxer
DJI system
I am not sure if anyone can help me, i am trying to figure out why 1 (back Left or Right) motor goes 100% and the other 3 motor stays the same when Throttle down 0%. This happens when trying to do a roll or pitch flip at 0% throttle (when i pump down after hard throttling up).....Here is the funny part, if i dont drop throttle to 0% and hold maybe ard 35%-40% throttle, the motor desync wont happen. Motor Idle too low?
link to BBL file - https://drive.google.com/file/d/1kUi...ew?usp=sharing
I do have BB log (link above) but im not sure if that will help. I took a screen cap to show exactly when it occured (refer below). I am unable to figure out what could be the problem and any input is much appreciated. Thanks!
mojo