06-Nov-2021, 09:54 PM
HI All,
Just finished building a 5" andI don’t seam to be getting any good punch out when full throttle, my drone with a battery is about 475g and I have 2208 motors which should be enough, when I full throttle it seams like if the motors aren’t spinning enough is there any limit or anything that could effect this ? I’ll attached my dump file and diff files. The only thing I can thnk of which I may have changed was the TPA breakpoint to 1350 but have now changed it back to 1650 but doesn’t make any difference, i'm going to reflash the fc and see if that makes any difference. If not im stuck at the min so any ideas would be welcome.
The stack im using is = http://www.holybro.com/product/kakute-f7-mini-v3/
and https://www.unmannedtechshop.co.uk/produ...ating=2450 in the 2450kv which should be enouth power.
thanks in advance.
Just finished building a 5" andI don’t seam to be getting any good punch out when full throttle, my drone with a battery is about 475g and I have 2208 motors which should be enough, when I full throttle it seams like if the motors aren’t spinning enough is there any limit or anything that could effect this ? I’ll attached my dump file and diff files. The only thing I can thnk of which I may have changed was the TPA breakpoint to 1350 but have now changed it back to 1650 but doesn’t make any difference, i'm going to reflash the fc and see if that makes any difference. If not im stuck at the min so any ideas would be welcome.
The stack im using is = http://www.holybro.com/product/kakute-f7-mini-v3/
and https://www.unmannedtechshop.co.uk/produ...ating=2450 in the 2450kv which should be enouth power.
thanks in advance.