14-Apr-2024, 02:04 PM
(14-Apr-2024, 12:48 AM)segler999 Wrote: When my 2S build did exactly the same thing as in the video, I simply changed the rpm filter in the PID tab. Don't change anything else; only the rpm filter. Slide the two sliders a bit to the left from 1.0 to something like 0.8, then try to take off. That worked for me.
Thanks, Segler999. I have done as you mentioned, but no effect on the drone. It flips over as I touch the quad just a bit (as in the video). Any new ideas? Tks.