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Quad flips on takeoff.
#16
So I went ahead and recalibrated the esc's and tested a few more times and unfortunately it made no difference.
I then tried to put foam on the bottom then the lipo on the bottom. Same thing.
Looked around online and saw a cli command
"set min_check=1150"
It seems to have fixed my issue. Motor 4 is still starting up a little bit slower then the others but it is much closer now. Went to the park with my son and flew three packs before dinner. Seems to handle good.
My next question is if I wanted to get the motor starting up as close as possible to the others do you think I should increase the min_check value more? Or would that not be the way to go.
Also I've never used the cli on clean flight before. Where can I find out the commands and more info on that. I'm totally comfortable with the command line on my Linux box at home so I'd like to learn more about it. Smile
Thanks for all the help and ideas and time everyone.
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#17
Here is a lot of info about the CLI

https://github.com/cleanflight/cleanflig...ocs/Cli.md
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#18
(06-Sep-2016, 07:32 AM)oyvinla Wrote: Here is a lot of info about the CLI

https://github.com/cleanflight/cleanflig...ocs/Cli.md
Thank you. I will check it out. Smile
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#19
Good you figured this out, but remember that below min_check you will have no control over yaw.
Find me on Youtube and Instagram. I currently fly: DRC Aura, NOX5R, Minimalist 112 and drive a scrap RC car
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#20
(06-Sep-2016, 08:14 AM)Konrad Stepanajtys Wrote: Good you figured this out, but remember that below min_check you will have no control over yaw.

Still trying to figure out what I'm actually doing. What do you mean by no yaw control. I dident notice any problems with it. Or perhaps I just dident see emWink
Is there a better command then min_check that I should use instead to get the same results??
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#21
Min_check is a value below which FC stops yaw output - it's used to avoid spins during stick disarm.
Find me on Youtube and Instagram. I currently fly: DRC Aura, NOX5R, Minimalist 112 and drive a scrap RC car
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#22
(06-Sep-2016, 09:06 AM)Konrad Stepanajtys Wrote: Min_check is a value below which FC stops yaw output - it's used to avoid spins during stick disarm.

Thanks for explaining it.
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