# diff all
# version
# Betaflight / MATEKF411 (MK41) 4.1.1 Nov 15 2019 / 12:34:58 (1e5e3d369) MSP API: 1.42
# start the command batch
batch start
# reset configuration to default settings
defaults nosave
board_name MATEKF411
mcu_id 002b00433339511838383538
signature
# feature
feature -DYNAMIC_FILTER
# map
map TAER1234
# master
set gyro_sync_denom = 32
set min_check = 1171
set max_check = 1828
set serialrx_provider = SPEK2048
set motor_pwm_protocol = OFF
set small_angle = 180
set deadband = 1
set pid_process_denom = 16
set usb_hid_cdc = ON
profile 0
profile 1
profile 2
# restore original profile selection
profile 0
rateprofile 0
rateprofile 1
rateprofile 2
rateprofile 3
rateprofile 4
rateprofile 5
# restore original rateprofile selection
rateprofile 2
# save configuration
save
# status
MCU F411 Clock=96MHz (PLLP-HSE), Vref=3.29V, Core temp=47degC
Stack size: 2048, Stack address: 0x2001fff0
Config size: 3570, Max available config: 16384
GYRO=MPU6000, ACC=MPU6000
System Uptime: 94 seconds, Current Time: 2020-09-18T22:37:47.105+00:00
CPU:4%, cycle time: 4005, GYRO rate: 249, RX rate: 91, System rate: 10
Voltage: 1 * 0.01V (0S battery - NOT PRESENT)
I2C Errors: 3
Arming disable flags: CLI MSP
Betafpv f4 aio 2s, BF 4.1 legacy.
Yes to saving after HID command, then it reboots and I am running BF while trying DRL.
I thought it was the gateway to using the FC usb, but will try giving the command + save, allowing the reboot and then close BF and open DRL.
After trying, nothing changed.