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9 02-Feb-2017, 04:28 PM (This post was last modified: 02-Feb-2017, 05:02 PM by Dutch Drone Builder.) Hello guys,
I have a question about my QX95 setup.
I have a cpu load of 0%, PID delta 990-1000, is this normal if it's on the bench?
Also i have 2 I2C errors.
If i move the quad the cpu load is still 0%
It's possible to fly the quad, it are just question out of curiosity
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139 have you tried flashing the firmware again (make sure it's the correct firmware target)
try to turn off unused I2C devices see if it fixes it? such as Baro and Compass (mag).
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30 I2C errors (afaik) happen during initialisation. As long as the number does not keep rising to infinity, you don't have to worry about that. At least that's what Boris said some time ago.
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30 PS: You could check "status" or "tasks" in CLI. Another possible reason could be that it's running an older firmware which didn't support realtime CPU display back then?
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9 04-Feb-2017, 07:43 PM (This post was last modified: 04-Feb-2017, 07:43 PM by Dutch Drone Builder.) I'm going to check your idea's i will report it back, and it's running now cleanflight 1.13 with the "problems"
Thank you for the idea's
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