27-Jun-2022, 01:51 AM
So I have this interesting build I’m working on. A custom Eachine Cvatar. I’m trying to configure a FlightOne MillivoltOSD flight controller with a BLHeli32 35a Eachine esc.
I want to double check my harness, but I’m almost certain it is all correct. When I plug in a LiPo, it beeps like normal. However, for some reason when on the bench A) I noticed I don’t have any voltage reading in BetaFlight for my LiPo which is full, and B) when I go to the motors tab to test and or configure the motors, I try to simply spin them individually with the sliders, and I have no movement in the motor, not even a stutter at all.
Now here’s a bit of info:
I have I actually double checked the harness and the one not thing I did mistakenly was wire my motors in a backwards order, so I might need to remap my motors when and if I get this working. Anyway, as for the MillivoltOSD flight controller, I have the esc protocol bridged for BLHeli_S with Current Sensor. I did wire my receiver to UART6, and maybe I should have chose a different one? I’m running Crossfire, but notice the F1 fc I think is using uart6 for esc telemetry? Would that cause an issue?
TIA everyone!? I’ve been wrestling with this for over a week now! I was able to flash the fc with BetaFlight 4.3 and everything up until now seems to be working fine!?
I want to double check my harness, but I’m almost certain it is all correct. When I plug in a LiPo, it beeps like normal. However, for some reason when on the bench A) I noticed I don’t have any voltage reading in BetaFlight for my LiPo which is full, and B) when I go to the motors tab to test and or configure the motors, I try to simply spin them individually with the sliders, and I have no movement in the motor, not even a stutter at all.
Now here’s a bit of info:
I have I actually double checked the harness and the one not thing I did mistakenly was wire my motors in a backwards order, so I might need to remap my motors when and if I get this working. Anyway, as for the MillivoltOSD flight controller, I have the esc protocol bridged for BLHeli_S with Current Sensor. I did wire my receiver to UART6, and maybe I should have chose a different one? I’m running Crossfire, but notice the F1 fc I think is using uart6 for esc telemetry? Would that cause an issue?
TIA everyone!? I’ve been wrestling with this for over a week now! I was able to flash the fc with BetaFlight 4.3 and everything up until now seems to be working fine!?